Success Stories 1. Food & Beverage Major Australian Bakery Rises with Low-Pressure Steam SteamAqua Offers Instantaneous Hot Water via Indirect Heating with Steam TLV Helps China Brewery Greatly Improve Equipment Reliability TLV supplies steam equipment to Ringwood Brewery TLV Provides a Sweet Solution to Tangerine's Hot Water Supply TLV valve improves heat transfer at Greencore site 2. Oil Refinery PETRONAS Refinery Achieves Significant Savings with Help of TLV & Enproserve Singapore Refining Company Teams Up with TLV for Major Energy Savings 3. Animal Feed Processing TLV to provide regular steam-trap surveys of all BOCM Pauls animal-feed processing sites 4. Textiles & Laundry Services TLV Helps Synthetic Leather Manufacturer Achieve Energy Savings Johnsons Stalbridge Linen Services' laundries utilize TLV steam pressure reducing system TLV's flash steam recovery system cuts launderer's costs and reduces emissions TLV monitors steam trap conditions at Sunlight 5. Logistics TLV Fixes Fukutsuka Transport's Water Heater Failure 6. Other COSPECT® Case Studies TLV vortex flowmeters for boiler steam monitoring TLV Steam Traps aid refurbishment of Marshall steam engine More Information Steam Theory Document Search Technical Documents Product Solutions CAD 3D Archived Documents Operation Animations Success Stories System Solutions FAQ PowerDyne® Disc Traps Email Magazine Discover steam engineering tips in our bi-monthly newsletter. Sign up now Singapore Refining Company Teams Up with TLV for Major Energy Savings TLV PTE LTD (Singapore) Working with TLV for almost ten years, Singapore Refining Company managed to achieve significant savings through improved steam trap management. Singapore Refining Company (SRC), one of three petroleum refineries in Singapore, was suffering from a large number of trap failures in 2003. A survey conducted by TLV showed that trap failure rate was around 50%. This represented significant annual monetary losses from steam leaks alone. Concerned with this high failure rate, the Energy & Loss Control Team at SRC worked with TLV to devise a plan for the gradual replacement of failed steam traps, including performance monitoring via steam trap inspections. To improve overall trap and plant reliability, part of the plan also involved the replacement of failed steam traps with TLV SS1 and JH5 Free Float® traps. The plan was put into action over the next few years, resulting in tremendous success. The steam trap failure rate had dropped to less than half in 2004 (compared to 2003) and progressively declined to reach an all-time low of less than 5% in 2010. The newly installed TLV traps played an important part in the plan. In low-medium pressure applications, only 1.4% of the new TLV SS1 steam traps failed within 5 years of service. In high pressure applications, only 3.9% of the newly installed TLV JH5 steam traps failed within 4 years of service. The Manager of Energy & Loss Control at SRC was very satisfied with the program. He added that TLV’s Trap Management System lead to “significant improvement in energy conservation through steam loss reduction and better steam trap performance.” The end result was that SRC was not only able to conserve a significant amount of energy and reduce its carbon footprint, but also achieve large savings through better steam trap management. Also on TLV.com What is a Steam Trap? Steam Trap Losses - what it costs you Steam Bulletin: Archive - Email Magazine